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HomeMy WebLinkAboutSWP2703497.8M 1 I- N U) a m O 0 0 U 01 O O N c m W 0 t M r N IS U Z 0 Of U w _ L madse C INSTALL TEMPORARY YPASS DAM S ra FOR C SON S SEE DETAIL =x `- ------------------- XN ACCESS FROM THIS PROVIDE SECOND DAM A ___ EEDEp IF TO AND PUMP •, L----- — -- ..\--------___COLLECT SECONDARY FLOW . ••. --____ A •'� —LOG DROPS PASS PIPE -K "CMP IE=121. UTILITY EASEMENT See Note UTILITY EASEMENT FROM NEW LIFE CHURCH 8/10/09 KING CO. RECORDING # 20091007000046 RECOMMENDED FOR APPROVAL BY Daniel Carey 6/30/10 BY 20 2H:1 V 16 BOTTOM OF BASIN APPX. EL 113 \ t 0' 2 0' O FF— Cn(� SCALE 1 "= 20 Feet = DE D = 0 x CONSTRUCTION NOTES 1. PIPE INVERT ELEVATIONS TAKEN FROM PRELIMINARY SITE PLAN, NEW LIFE CHURCH, WEST SIDE IMPROVEMENTS. 2. SEDIMENT LIMITS AND BASIN BOTTOM ELEVATIONS ARE APPROX. THE CITY MAY ADJUST THE SEDIMENT REMOVAL LIMITS AND DEPTHS AS NEEDED. REMOVE SEDIMENT TO BASE GRADES SHOWN 3. TEMPORARY BYPASS DAM SHALL BE WATER TIGHT SO BASIN OR TO TOP OF RIP —RAP ON SIDE SLOPES. CAN BE DRAINED AND SEDIMENT CAN BE DRIED OUT. HAND DIG IF NEEDED TO IDENTIFY RIP —RAP. DO NOT OVEREXCAVATE SIDESLOPES. 4. FISH RESCUE IN THE SEDIMENT BASIN SHALL OCCUR USE SMOOTH BUCKET, NO TEETH. IMMEDIATELY AFTER THE BYPASS DAM IS INSTALLED. \ . \ ' SEDIMENT LIMITS APPROXIMATE. ACCESS B,gSIN DOWN TSI \� -'� i SEDIMENT DEPTH APPROX 4 TO 6 FEET. ( I ICE \ LY Li 24"CMP BYPASS PIPE LOCATION NOT VERIFIED,"",, 2 P ` \ ' I 120 A \ �'°'� uj m D , / X HYDR EED A D STRAW MULCH \0q�`� ISTUR D SL E AND ACCESS ROAD AIT B IN CL NING 12'x3' CONC. BOX CULVERT 24"CMP BY ASS PIPE ` LOCATION OOT VERIFIED l BYPASS PIPE OUTLET 24" CMP IE=116.12 OVERFLOW SPILLW Y IE=117.86 UTILITY EASEMENT ,x NO See Note ACCESS FROM T I S S IDE 36" CMP INLET ' IE=115.81 ('V X. ... ... GRA .......- DEL q00 '-- - \- ` \ oVERF _-_ ESS �oW C RO aN ' - AD 36" CMP OU'RLET \�� EL (d,y) _ IE=114.47 �\ �� OVERFLOW SPILLWAY IE =116.8 est ` O - \n \30 r .. co � S ` CD ,Q O SEDIMENT BASIN CLEANING DRAWING OM SR— 9 AS -BUILT NOTES 1. 2009 — POND BOTTOM WAS WET AND MUCKY. EXCAVATOR STAYED ON PAD OF SEDIMENT AND REMOVED MATERIAL TO APPX. EL 113 BY JUDGING THE DEPTH SHOVEL WENT DOWN. APPROX 1000 CY REMOVED. BOTTOM WAS TOO MUCKY TO WALK ON AND SURVEY AFTER WORK WAS FINISHED. 2. 2010 — POND CLEANED TO APPX EL 113. BOTTOM WET, MUCKY DUE TO WATER GETTING PAST DAM OR GROUNDWATER. D-349105 SURVEYED: SCALE: VERTICAL: NAVD 1988 DESIGNED: AS NOTED HORIZONTAL: NAD 1983/1991 41 _ CITY OF %'� DRAWN: °° ML F ENTON DC ONE INCH DATU M CHECKED: AT FULL SCALE Planning/Building/Public Works Dept. DC / RS IF NOT ONE INCH NO. REVISION BY DATE AP P R APPROVED: IRSSCALE ACCORDINGLY 2011 Cleaning 6/30/11 MADSEN CREEK SEDIMENT BASIN FIELDBOOK: PAGE: CLEANING PROJECT DRAWING N0: SEDIMENT BASIN 1 SHEET: OF: x 2 U-13 419171 1