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LAKE FRONT SANIlArMllf COLLECTION i
SIDE SEWER IMPROVEMENT PROJECT
VICINITY MA P
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Horton Dennis fay' Associates, Inc.
10 Consulting Engineers
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- APPROVED B7 TOR OF KuiifLS
Job No. 548j
LAKE WASHINGTON
A 11e1'ae1o1;,s /a F /ush S1'5'11017
r I\ l
ra +p0 ® • •
•
®•
,--Bross Tag (Typ.)
! ! .efte. 8 +00
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I 2805 ��
I 2801 1 1 1 28 D _ 4 J °1 LJ
��„ (
27 L — T --',� i - 1
L2727 -bis J 2827 �
_
F /u3h5fation w� � ®r 1��tt ®�T %B� i 2815
®1A o�0�[[Lo• ®�b®®6° 2 +04
Sta 0 +00 --
Begin Project - - -- - - -- -- e N. ----- - - - - -- - - - - - -- —
_ Avenu ----- - - - - --
'- hit. V -- - -- - --
- -- ' - - - - -- 1 -- --------------
- - - - - -/ - -- -- ----- - - - - -- -- - 2 V
LEGEND Disclaimer:
Ra ®r ®� Existing 8' CI Sewer Line The asbuilt .survey of the sewer line was completed using electronic - - - - -___ - -
g pipe locators and steel probes. Although every effort was made to
accurately locate and profile the sewer line, the information shown --
- — — -- Existing 6' 8 4' Side Sewers .. is approximate and has been drafted on'existing plan /profile sheets
® originally prepared by others. The information shown on the plan views -
®� Exit 'ing..Sewer Clean Outs (located) hes not been surveyed or tied to any known property corners.
8... Detail Letter
� Sheet Number
Flush Station
�Approx. Exis/`iiiy �rour�n'.Sur'face
Top EL 20.1 � -3/ 28/5
F.F. Z827 40" -1 F.FF /T9.6 — I'- - - -__ .._�_ - -__.. IE /./y.51 rFFEI. /9.41
J Ground El. 17.7
S
Roy
Dl+TUM —
U.S.C. a GS.
Datum Conversion Equation:
U.S -C.E. Lake Level — 6.82 feet = US.C. a GS. Lake Level
\
i0 +00
1
00000 0o ppO00 100�� Co %man
.n KENNYDALE SEWER LINE
Point
i0
\
�`S �
0y
n
a\a / / �O
% I
I
\- -- _ High Lake Level 15.2
Inv. 15.8 Low Lake Level 13.2 Top Of, Exist. 8 C. / P, 6xisfh7q Lake Bed
N
g
4 No Sleanouts Found Pi e Exposed v
Sewer Depth Shawn is Approx. �- -Pipe Exposed
Summary of Work to Be Accomplished
Under This Contract
Detail Letter
Total This Sheet
Detail A
/
Detail B
/
Detail C
Z
Detail D
6
Total Work Items
This Sheet
��
PENyy -
d P of WASH /a� FQ
m
0
��.of,�F6 /STEA�O� ?4r�a 'Z �0,c'PfG15fEQ'�G2�4.
_ 4 0 p p _ ® O
20
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/2
8
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Horton Dennis f3' Associates, Inc. CITY OF RENTON DAT� // -SG 5483.0
Consulting /" =40'4 SANITARY SEWER L.I.D. 270
Consulting Ene' °` ®`� PUBLIC WORKS DEPARTMENT [DA�[, "¢'V [M[lTNo.
Aar[DV[D OAT[ SIDE SEWER IMPROVEMENT PkGjtCT 2 °,
c[[o .4 E/ri [T "[o� R[ v 1 8 1 o N sr S E A T T L E. W A S H I N G T O N
v I say 14 * ♦
�►�rw♦ rrr rrrr +�r \` Qrr ie �� \\ �\ ♦♦ x
,gal \
\ `. 013 \ \� � � \ \� � � 3 /r � 1 ♦ Z
eat �1 _ �,p ,.rte ®tea - - - - --
LEGEND o \ 3j61 ' \\\ 3119 3205 32, -- - - - -- 1 — ----
-� --- - - - - -- - - --
\ / \ \fig - - - - - --
®�r�® Existing 8° Cl Sewer Line � \ � -- `- __ - -- ---- --
,
r
- - - °- - --' -
Existing 6' $ 4' Side Sewers - - - - -- - -- - tv
Existing Sewer Clean Outs (located) g 1 "_ ". - " -- - +
Detail Letter
W
B -- N � , `. ,, � 103
Sheet Number 3 \0� \ `, ' i tle prthPln R ;
-� \ \`, �, 3 peen N `,
--- - - - - -- ---- - - - - -- - - - - --
��pl Lake Washington Blvd. --------- - - - - --
!DATUM — --- __ - - --
Disclaimer:
U.S.C. Se GS. O�y _ - -'- The asbuilt survey of the sewer line was completed using electronic
O1 pipe locators and steel probes. Although every effort was made to
�� _ accurately locate and profile the sewer line, the information shown
DQYUtn Conversion Equation: _ s approximate and has been drafted on existing plan /profile sheets
`` \\ originally prepared by others. The information shown on the plan views
U.S.C.E. Lake Level — 6.82 feet = US.C. & GS. Lake Level has not been surveyed or tied to an known I
y y property corners.
En
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LEM- �.. ,oe o.
—_ Horton Dennis f�' Associates, JTnc. CITY OF RENTON n a� KENNYDALE SEWER LINE 5;
o� �Hro. AE Al
oaawr+ ✓�� ', Consulting Engineers PUBLIC WORKS 'DEPARTMENT � 40 -,� ` s..Err.�n.
_ SANITARY SEWER L i D 270
__ -- -ON - - - -. - -- - o.. S E A T T L E, W A S H I N G T O N - SIDE SEWER IMPROVEMENT PROJECT. 3 �F. 6
<H -r. AEN/ s,Meo R E v 1 5 1 e, o oar.
4
10
. 1A 36,-ju
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je. % �t\
LAKE WA,5HpVG—,0Air
3L-1)
use a GS, 2*00 'WO04,609010 p
Datwr Comversion Equolion; 60m .0.. no so to 6
USC E. Lake Level — G$2 feet 9 USC a GS Lde Level _mp. _ lv�
30#00
2
24*00 &as 5 rep (lyp
map 8 #00
24.00 00 0 •
Kennydele
&-och porl(
Got
i I 10_7% fn
0401 p
I Z
1307
Pipe E.FC,5,ea
$Wmry of work to Ile Accomlish"
muter This CoAt"Ct
kt4i) letter
Tatik) This Ueat
Detail C
Detail D
I
(a
Surleeco- 1r7
2
covxrt-te ftult
9
tM
----- ------------------
ton e2b14.
Disclaimer:
a- C, se-W unt
The asbuilt survey of the saver lint was completed using otge ronte
ExIdIft V & 4V swe So""
pipe IQCators and steel prob*x. Although *v*ry effort wa§ made
accurately locate and profile che sow, line. the Infur,ation "'In
EWSWV Seow Dow 04ft 0000"
1:j&VPr0x1mat* and has betn drafted on wxt�%ctng ptAn/peciija gh.0
0 g1*311Y PrtVac*d by others. The Inf0fMAti—
shown 0.1 the pjaont�',L..s
has not b*en surveyed Or tied .0 any known pr+l ptrty cot,
.Orq.
1307
Pipe E.FC,5,ea
$Wmry of work to Ile Accomlish"
muter This CoAt"Ct
kt4i) letter
Tatik) This Ueat
Detail C
Detail D
I
(a
—1
4001 k
2
Tau] ftft 11%%
This 3b"t
9
tM
orton Dennif Z!r Arfocijief. Inc CITY OF RENTON KENNYDALE SEWER LINE 17 ix Aff -
SANITARY SEWER LID 270
i"^OVS MCDARTMENT
PUBLIC Ty will. Lf%_V
SIDE SEWER IMPROVEMENT PROJECT 4
)jp I
4
0
tM
orton Dennif Z!r Arfocijief. Inc CITY OF RENTON KENNYDALE SEWER LINE 17 ix Aff -
SANITARY SEWER LID 270
i"^OVS MCDARTMENT
PUBLIC Ty will. Lf%_V
SIDE SEWER IMPROVEMENT PROJECT 4
)jp I
4
0
lr���ea�r
LAKE WASH /NGTOAI
38 +00 40 +00
\ I
� ; I
� o
G \
Not Located
/x00 See Constr
No fe /O, Sh• Cc
Bro55 Tag
I
DATUIrf -
5co e I
U.S.C. & GS.
Datum Conversion Equation:
D k\ I US.C.E. Lake Level — 6.82 feet = US.C. a GS. Lake Level
�\\� lJ I 1 Nate
9, \\ 5 ill �. \\ 3815 I See ConsfV7. 6 �
\ Note B, Sh. G
\ \ JI �O I neck s% _� D ( / 383 Overflow /!o " C. L Pipe
\ 1 i 3711 311 319 `.% , 6 I 3821 3825 `� -- ,
% -\ 03 \\ e , 3915 , ° , - - - - - -- , _ k' �; c.o
3' �> fag !, ,` - - -' -- �_y -_`' °^L. \ Lift Station
d �lq I C>° - ------- - - - - -- - - -_ 3827
3 323 _ 3�0 _ _ Puf Rood _ _
r- te_ "- f- L.
-�� -�- - �'- - - - -- i
It
i 'I
� � — — — — — •— — — — — — — -- — — — — — — — - -- — `' —� •9 il'9etro ��(20° S/ee/ C�Si/1yJ
Lgfe tYoshrri f -ems jj(
Monhole
IL
t
20
LEGEND Disclaimer: - - _- --
The asbuilt survey of the sewer line was completed using electronic
- -a -- Existing 8' Cl Sewer Line pipe locators and steal probes, Although every effort was made to
accurately locara and profile the sewer line, the information shown
IA approximate and has been drafted on existing plan /profile sheets
originally prepared by others. The information shown on the plan views
has not been surveyed or tied to any known property corners.
-- -- Existing 6' 8 4' Side Sewers
Existing .Sewer Clean Outs (located)
B Detait L
6 Sheet Number
3707
F. F
48, Pr e Exposed .. E/er.,5S _
Pipe Exposed
- -_ _ Hr,Zh Lafre .eve✓ /5.2 --
Lowy Luke I eyer 13.2
12
�t
Er 197'. Lwlie Beck -,row ' 0, Gr /S't 8 G. /. P
v
.�
S
O
tt
Pipe Exposed
Si mory -of -Work to Be Accomplished
Under This Contract
Detail Letter
Total This Sheet
Detail 0
9
Detail E
I
Total Work Items
This Sheet
10
D
O
r
20
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12
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Horton Dennis f9'' Associates, Inc. CITY OF RENTON KENNYDALE SEWER LINE I °•
LSANITARY SEWER L.I.D. 270 - 5 Consulting Engineers .._.._..___ __..___ ___, _. S E A T T l E. W A S k 1 N 6 T r U6LiC WORKS DEPARTMENT SIQE SEWER IMPROVEMENT PROJECT ._ f Y 1 4 J ow.
N ev a„CnrCn L�rL
Vj
ALTERATIONS_ TO
EXISTING FLUSH STATION IA
No ITCa /e 6
o
PLAN VIEW
F _ -
— �'�orrsnre-
Con
Roc
' I,
I.
LONGITUDINAL SECTION A —A
8•,
8" CI Retainer
G /ands A
Exist. 9 D P/*
Materials Required:
2 - Expose and Confirm Sewer Location
1 - Remove 8" D.I. cieanout and return to .City.
1 - 8' 0.1. 45° Bend NJ x MJ
1 -..8 x.10.0.1. Concentric reducer NJ xFL .. _......
.1 - 10" D.I. Solid sleeve 48 "s long FL x PE
1 - 10" Insta - Flange.
1 - 16" x 6" Regular reducing flange with 12 bolts and nuts to fit —
Clow F -1905 or approved equal,
st. Grade 1 - 4k• NST bronze pumper nozzle and CI cap and fittings to fit nozzle into 6"
reducing e.
i - 1 Cu. Y . flangconcrate `thrust block
1 - 1 Cu. Yd. 3/4" minus compacted crushed rock
1 - 24 x 2' concrete pipe section
1 - Manhole ring and cover to be 24" clear opening, with bolt down
(locking lid) ring and cover equal to Olympic Foundary No. 5943 WS -L.
Cover shall have wording, "SEWER" for sanitary sewer.
2 - Cut existing 8" Cl pipe.
1 - 8" DI. Clow F -1220 Cutting-in-sieeve-
1 - 8" CI AWWA resilient wedge valve MJ x MJ with CI valve box and valve
nut extension per Renton Standards.
2 - 8" DI Retainer glands.
'r 3/4 "�ttinus
cted Crushed
�l� -Exist B" �S° Bug'
`�-- Exlst. e "DI Wye
,rExist. 8 "�I P/pe
Piping to be Air Tigh'
lvith no Leaks of
150 A5.I when Plag Y,?*e
is Closed
VIII New I�IIINew .Sleeve (I -
Exist. - Re /ocated a
6 - CI Nye -Add Retainer
G /ar�ds
Shorten, Re/ocata e Reconnect
Exlsf 4" or G" Si e- .Sewerls).
Odd Ne v Clean Outs on Side _
Sewers as Req'� by Health
h'e9u/afion.3.
SIDE—SEWER-PLUG-VALVE
INSTALLATION DETAILD�
No Scale 6
Materials Required:
4 - 6" DI Retainer Glands
Clow F -1058 or Approved Equal
1 - 6" DI Sleeve 24" Long MJ X MJ
1 - 6" X- Centric Plug Valve-MJ X MJ
inc. CI Valve Box and Lid.
1 - 0.5 Cu. Yd. Concrete Thrust Block
Exist. Ya /" /-N
Box
/- Exist; 6"
CI Pioe
oncrete
t. R;p Rc
t4c7ke
sPy
/nyn To La/re
Line
Materials Reauired:
2 - Cut existing 6" Cl pipe (2 places) and remove pipe..
1 - 6" X- Centric Plug Valve MJ X MJ inc. Cl valve box.
1 - 6" DI Retainer gland.
1 - 6" DI MJ Cutting in sleeve with set screws
Clow F -1220 or approved equal.
1 - 0.5 Cu. Yd. Concrete Thrust Block
SiDE SEWER CUT iN PLUG VALVE
-INSTALLATION DETAIL E
No Scale 6
CONSTRUCTION NOTES:
1. ALL SITE.._..AND__DTILITY .WORK TO BE COMPLETED TO THE CITY OF RENTON,
- --
DEPARTMENT OF PUBLIC WORKS STANDARDS.
2. CONTRACTOR TO VERIFY LOCATION OF ALL UNDERGROUND UTILITIES BEFORE
.STARTING CONSTRUCTION.
3. A 24 HOUR NOTICE SHALL BE GIVEN TO THE RENTON POLICE AND £IRE
DEPARTMENTS IH THE EVENT OF STREET OR WATER MAIN CLOSURES.
4. OWNER SHALL STAKE THE LOCATION OF EACH PLUG VALVE TO BE INSTALLED.
5. ALTHOUGH NO PRESSURE TESTING WILL BE REQUIRED FOR THIS CONTRACT,
SUBSEQUENT PRESSURE CLEANING OF -THE LAKE LINE BY OTHERS WILL
PRESSURE TEST THE IMPROVEMENTS COMPLETED IN THIS CONTRACT. THE
CONTRACTOR FOR THIS CONTRACT WILL BE RECALLED TO CORRECT LEAKS OR
FAILURES IN HIS WORK, AT NO COST TO THE CITY, THAT OCCUR UP TO 150
PSI TEST PRESSURE.
6. ALL PVC SEWER PIPE INSTALLED UNDER THIS CONTRACT SHALL BE MARKED
WITH METALLIC LOCATING TAPE 12 INCHES DEEP,
7. ALL FINISHED SLOPES SHALL NOT EXCEED. 3:1.
8. CONTRACTOR SHALL RESTORE ALL DISTURBED AREAS TO MATCH
PRECONSTRUCTION CONDITIONS AS DETERMINED BY THE OWNER'S INSPECTOR.
PROJECT PHOTOGRAPHS AND VIDEO TAPE WILL BE USED TO VERIFY PROPER
RESTORATION.
9. .AT 3901 LAKE WASHINGTON BLVD. NORTH, THE CONTRACTOR SHALL ADD ONE j
6" WYE AND CLEAN OUT JUST UP STREAM OF THE NEW PLUG VALVE UNDER E
THE EXISTING DECK. CONTRACTOR SHALL RESTORE THE WOOD - DECKWITH A
NEW REMOVABLE DOUBLE FRAMED 4'X4' WOOD ACCESS HATCH BUILT INTO THE
-
DECK AND SUPPORTED- AS REQUIRED. - - -
10. AT 3715 LAKE WASHINGTON BLVD. NORTH, THE CONTRACTOR SHALL RESTORE
THE "WOOff DEM NiTa A.. NF —,F.. REMOVABLE - DOUBLE FRAMED. 4'°n ewD ACCESS
HATCH BUILT INTO THE DECK AND SUPPORTED AS REQUIRED.
11. WITH THE OWNER'S INSPECTOR PRESENT, THE CONTRACTOR SHALL EXPOSE
THE SIDE SEVEN, LOCATED BETNEW 3811 AND 3815 LAKE WASHINGTON BLVD.
NORTH, AND VERIFY. THAT THE SIDE S :'ERS FOR THESE HOMES ARE
COMBINED INTO ONE 6" SEWER LINE DRAINING TO THE MAIN 8" LAKE
SEWER.
12. 'ALL RETAINER GLANDS SHALL BE INSTALLED PER MANUFACTURER'S
DIRECTIONS USING A TORQUE WRENCH. _
13. EXTRA WORK AUTHORIZED BY THE CITY BUT NOT COVERED UNDER THE
CONTRACTOR'S PROPOSAL MAY BE COMPLETED AS A FORCE ACCOUNT ITEN AS
DEFINED IN SECTION 1 -09.6 OF THE STANDARD SPECIFICATIONS.
SEWER PIG ACCESS PIPING DETAIL,, B
/YO 604 1e 6
\fit. wEN//� i6,i�.re yiC �a
Q �toF 'KMip�, fF.z d" q VIM,,v` F,P
i�
STEP�'6\�a�<,, ,r �� •�FCrSrERCa . �, r
ANAL t�'!�' =c SSrg��..�N'"C,'\�'',',
Boa "o.
Horton Dennis Cr Associates Inc. CITY OF, RENTON KENNYDALE SEWER LINE i
� —^ orr� �� -� SANITARY SEWER L.I.D. 270
-- —
- -- - - --
Consulting Engineers PUBLIC WORKS DEPARTMENT -_ ° °A�6 ^'�
BRA -- � -- -- - - - -- -- DETAIL SHEET
A
�n,� K I R K L A N D, WASH I N G T O Nw"n"ovxo
�/�' /_ _ R E V 1 5! O N 8Y PxOYEO OAi6 ___-
Remove Existing Flush Station Piping and Add the Following
New Fittings Required Between Points A and B
See No%
B 1 - B" x 4" DI Concentric Reducer FL X FL -
to Right
1 - 8" DI Elbow FL X FL Materials Required:
New 1 - 8" DI Tee FL X FL
P /pin 1 - DI Reducing Flange 4" X 131" 2 - 8" D.I. Retainer Glands
i
Clow F -1905 or Approved Equal with
tCuanYd�uConcreteQuired __to.secure clean out cover.
72"
4 - 4" Galv. Threaded ach Tins and Thrust Block
S' -* 8 Prp by 4 - 4" Galv. Nipples Each Lon for Adjustable Overflow Pi 1 0.5
1 - 8" DI Pipe FL X MJ 8' ±- Long to Fit
Exist / "CI
6 "Min.
1 - 8" Flexible Coupling
P
Pipe and
New
8':fI Clp Out
Piping
Add F /ex Exist. 8 "Ac/
CauAling
A
Set Nety 8"01 Add Retainer -�
—
Pipe in 1Yon- .1h1/7k G /ands o Secure °
Exist.
Grout C.0, Coyer avrlh
4 "Piping
Lake
APprox. Lake leyel Bolts a// Arau �a °
36..
Move Exist Pump
to left
as Req'cJ to Meet
31 lY4 // C /earonce
Frvrn Lake
INash/nyton —_ --
P/pe at LoWer End SINGLE" SIDE SEWER CLEAN OUT COVER
as R�tJ to Fit
New Pipiny RESTRAINT INSTALLATION DETAILC
No Sca /e 6
ALTERATIONS_ TO
EXISTING FLUSH STATION IA
No ITCa /e 6
o
PLAN VIEW
F _ -
— �'�orrsnre-
Con
Roc
' I,
I.
LONGITUDINAL SECTION A —A
8•,
8" CI Retainer
G /ands A
Exist. 9 D P/*
Materials Required:
2 - Expose and Confirm Sewer Location
1 - Remove 8" D.I. cieanout and return to .City.
1 - 8' 0.1. 45° Bend NJ x MJ
1 -..8 x.10.0.1. Concentric reducer NJ xFL .. _......
.1 - 10" D.I. Solid sleeve 48 "s long FL x PE
1 - 10" Insta - Flange.
1 - 16" x 6" Regular reducing flange with 12 bolts and nuts to fit —
Clow F -1905 or approved equal,
st. Grade 1 - 4k• NST bronze pumper nozzle and CI cap and fittings to fit nozzle into 6"
reducing e.
i - 1 Cu. Y . flangconcrate `thrust block
1 - 1 Cu. Yd. 3/4" minus compacted crushed rock
1 - 24 x 2' concrete pipe section
1 - Manhole ring and cover to be 24" clear opening, with bolt down
(locking lid) ring and cover equal to Olympic Foundary No. 5943 WS -L.
Cover shall have wording, "SEWER" for sanitary sewer.
2 - Cut existing 8" Cl pipe.
1 - 8" DI. Clow F -1220 Cutting-in-sieeve-
1 - 8" CI AWWA resilient wedge valve MJ x MJ with CI valve box and valve
nut extension per Renton Standards.
2 - 8" DI Retainer glands.
'r 3/4 "�ttinus
cted Crushed
�l� -Exist B" �S° Bug'
`�-- Exlst. e "DI Wye
,rExist. 8 "�I P/pe
Piping to be Air Tigh'
lvith no Leaks of
150 A5.I when Plag Y,?*e
is Closed
VIII New I�IIINew .Sleeve (I -
Exist. - Re /ocated a
6 - CI Nye -Add Retainer
G /ar�ds
Shorten, Re/ocata e Reconnect
Exlsf 4" or G" Si e- .Sewerls).
Odd Ne v Clean Outs on Side _
Sewers as Req'� by Health
h'e9u/afion.3.
SIDE—SEWER-PLUG-VALVE
INSTALLATION DETAILD�
No Scale 6
Materials Required:
4 - 6" DI Retainer Glands
Clow F -1058 or Approved Equal
1 - 6" DI Sleeve 24" Long MJ X MJ
1 - 6" X- Centric Plug Valve-MJ X MJ
inc. CI Valve Box and Lid.
1 - 0.5 Cu. Yd. Concrete Thrust Block
Exist. Ya /" /-N
Box
/- Exist; 6"
CI Pioe
oncrete
t. R;p Rc
t4c7ke
sPy
/nyn To La/re
Line
Materials Reauired:
2 - Cut existing 6" Cl pipe (2 places) and remove pipe..
1 - 6" X- Centric Plug Valve MJ X MJ inc. Cl valve box.
1 - 6" DI Retainer gland.
1 - 6" DI MJ Cutting in sleeve with set screws
Clow F -1220 or approved equal.
1 - 0.5 Cu. Yd. Concrete Thrust Block
SiDE SEWER CUT iN PLUG VALVE
-INSTALLATION DETAIL E
No Scale 6
CONSTRUCTION NOTES:
1. ALL SITE.._..AND__DTILITY .WORK TO BE COMPLETED TO THE CITY OF RENTON,
- --
DEPARTMENT OF PUBLIC WORKS STANDARDS.
2. CONTRACTOR TO VERIFY LOCATION OF ALL UNDERGROUND UTILITIES BEFORE
.STARTING CONSTRUCTION.
3. A 24 HOUR NOTICE SHALL BE GIVEN TO THE RENTON POLICE AND £IRE
DEPARTMENTS IH THE EVENT OF STREET OR WATER MAIN CLOSURES.
4. OWNER SHALL STAKE THE LOCATION OF EACH PLUG VALVE TO BE INSTALLED.
5. ALTHOUGH NO PRESSURE TESTING WILL BE REQUIRED FOR THIS CONTRACT,
SUBSEQUENT PRESSURE CLEANING OF -THE LAKE LINE BY OTHERS WILL
PRESSURE TEST THE IMPROVEMENTS COMPLETED IN THIS CONTRACT. THE
CONTRACTOR FOR THIS CONTRACT WILL BE RECALLED TO CORRECT LEAKS OR
FAILURES IN HIS WORK, AT NO COST TO THE CITY, THAT OCCUR UP TO 150
PSI TEST PRESSURE.
6. ALL PVC SEWER PIPE INSTALLED UNDER THIS CONTRACT SHALL BE MARKED
WITH METALLIC LOCATING TAPE 12 INCHES DEEP,
7. ALL FINISHED SLOPES SHALL NOT EXCEED. 3:1.
8. CONTRACTOR SHALL RESTORE ALL DISTURBED AREAS TO MATCH
PRECONSTRUCTION CONDITIONS AS DETERMINED BY THE OWNER'S INSPECTOR.
PROJECT PHOTOGRAPHS AND VIDEO TAPE WILL BE USED TO VERIFY PROPER
RESTORATION.
9. .AT 3901 LAKE WASHINGTON BLVD. NORTH, THE CONTRACTOR SHALL ADD ONE j
6" WYE AND CLEAN OUT JUST UP STREAM OF THE NEW PLUG VALVE UNDER E
THE EXISTING DECK. CONTRACTOR SHALL RESTORE THE WOOD - DECKWITH A
NEW REMOVABLE DOUBLE FRAMED 4'X4' WOOD ACCESS HATCH BUILT INTO THE
-
DECK AND SUPPORTED- AS REQUIRED. - - -
10. AT 3715 LAKE WASHINGTON BLVD. NORTH, THE CONTRACTOR SHALL RESTORE
THE "WOOff DEM NiTa A.. NF —,F.. REMOVABLE - DOUBLE FRAMED. 4'°n ewD ACCESS
HATCH BUILT INTO THE DECK AND SUPPORTED AS REQUIRED.
11. WITH THE OWNER'S INSPECTOR PRESENT, THE CONTRACTOR SHALL EXPOSE
THE SIDE SEVEN, LOCATED BETNEW 3811 AND 3815 LAKE WASHINGTON BLVD.
NORTH, AND VERIFY. THAT THE SIDE S :'ERS FOR THESE HOMES ARE
COMBINED INTO ONE 6" SEWER LINE DRAINING TO THE MAIN 8" LAKE
SEWER.
12. 'ALL RETAINER GLANDS SHALL BE INSTALLED PER MANUFACTURER'S
DIRECTIONS USING A TORQUE WRENCH. _
13. EXTRA WORK AUTHORIZED BY THE CITY BUT NOT COVERED UNDER THE
CONTRACTOR'S PROPOSAL MAY BE COMPLETED AS A FORCE ACCOUNT ITEN AS
DEFINED IN SECTION 1 -09.6 OF THE STANDARD SPECIFICATIONS.
SEWER PIG ACCESS PIPING DETAIL,, B
/YO 604 1e 6
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Boa "o.
Horton Dennis Cr Associates Inc. CITY OF, RENTON KENNYDALE SEWER LINE i
� —^ orr� �� -� SANITARY SEWER L.I.D. 270
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Consulting Engineers PUBLIC WORKS DEPARTMENT -_ ° °A�6 ^'�
BRA -- � -- -- - - - -- -- DETAIL SHEET
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