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HomeMy WebLinkAbout20180398E003 Renton ES 16 2022-06-27 FR 030 Kirkland | Tacoma | Mount Vernon 425-827-7701| www.aesgeo.com Date Mailed: Principal / PM: Bruce Guenzler, L.G., L.E.G. This document is considered a DRAFT until signed or initialed by an AESI Principal or Project Manager Page 1 of 2 v.7.20 FIELD REPORT Date Project Name Project No. Report No. 06/27/2022 Renton Elementary School 16 20180398E003 030 Location Municipality AESI Project Manager AESI Field Rep 1075 Duvall Ave NE Renton Bruce Guenzler, L.E.G. Bruce Guenzler, L.E.G. Permit No. Client/Owner Attn Requested By B21004604 Renton School District No. 403 Ed Thomson Client Engineer/Architect General Contractor Grading Contractor Weather CPL / Hutteball + Oremus Cornerstone/Kyle Continental Dirt Contractors/ Jerry Jr. Sunny, 80’s THE FOLLOWING WAS NOTED: Grading North (Sketch areas 1, 2, 3): CDC is continuing to pull wetter than optimum soil from the stockpile (Area 1), pre – dry the soil by aerating and turning with a disc in Area 2, then moving the pre – dried soil to Area 3 for placement and compaction. We observed compaction of the current lift in Area 3 by watching the smooth drum vibratory roller. Area 3 was firm and unyielding and ready for the next lift of soil in our opinion. At about noon today the remaining fill to reach plan grade in Area 3 visually appeared to be about 2 to 3 feet. The current process and sequencing of the soil drying operation is working very well and assuming weather continues to be dry excellent progress is expected. Plumbing-Electrical Conduits (Sketch Areas 4 and 5): Most of the trenches for the plumbing and electrical lines are shallow (less than 1 foot) and were excavated in the building pad rock (2-1/2 inch minus crushed rock). AESI made visual and t-probing observations during compaction at random locations. Subfloor electric and plumbing backfills observed in Areas 5 and 6 today appeared firm and unyielding and suitable for support of the floor slab, in our opinion. Water Tie In (Sketch Area 6): A fire loop water tie in was in progress at the northeast site corner. The area had been excavated approximately 8 feet deep and a water tap was being observed by the City inspector. No backfill was placed today. Conclusion AESI will return tomorrow morning to review progress on geotechnical aspects of construction. 6 Date Project Name Project No. Report No. 06/27/2022 Renton ES 16 20180398E003 030 Page 2 of 2 FIELD REPORT Sketch (See text for Area notes):